Monday, April 10, 2006

April 10, 1963 -- Loss Of USS Thresher

Forty-three years ago today, USS Thresher (SSN 593) was lost during sea trials with 129 riders and crew. Portsmouth Naval Shipyard marked the anniversary this weekend with a solemn ceremony. While the sinking of Thresher remains a cause of mourning within the Sub Force, we can take solace from the fact that the boat's loss spurred the development of the SubSafe program, which I believe has been one of the main reason we haven't lost any boats since USS Scorpion (SSN 589) in 1968 -- the program wasn't fully implemented in time to save her.

To the families of the 129 men lost aboard Thresher -- their sacrifice was not in vain. We continue to honor them along with all Submariners still on Eternal Patrol.

Update 0623 11 April: Here's a new American Heritage article on the loss of the Thresher. From this page, I also found a pretty good article on the history of submarine escape systems from 1986.

2 comments:

  1. Hi. It ate my first post so this one is shorter. I'll be home in about an hour.Right now we're in Health learning about diabetes. I have a project due on the 24th. You had better remember dad.

    That is all, deepdiver

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  2. While Googling the 50th anniversary of the Thresher sinking, I came upon this:

    https://www.designed4submariners.com/Thresher_Loss_Analysis.html

    As poorly written as it is, this raises some interesting questions:

    *Could you really determine the status and health of an electrical bus based on acoustical analysis of cooling pump speed?

    *...especially using the technology of the day (limited computing power.)

    *...and isn't it convenient that the original recordings were destroyed?

    *...and if there were an electrical problem, wouldn't you think the CO would stop the dive until the problem was located? As an ex-ENG, he would know all too well the hazards of scramming out at or near test depth.

    *If there was no pipe rupture, why did the sub sink? It suggests that the ship had negative buoyancy on a deep dive after overhaul - which seems like insanity.

    Anyway, it's an interesting take. It seems to exonerate the workmanship at Portsmouth - which may be the idea.

    What do you think of this? I noted elsewhere that Norman Polmar cited this analysis in a shot he took at the current director of NR (why is Polmar still whizzed at NR? DId they cancel a ride he was to take?)

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